The Fix? Unfortunately this is one of those cases where new parts and careful assembly won’t make it better. The system is stressed and will fail if used and not corrected. With the help of my dear friend, Mr. Charles – we set about finding a solution.
Careful study confirmed that we could not simply add more pins since the roller assembly that engages the crankshaft has slotted tunnels with spring plungers that don’t leave room for a 2nd or 3rd knock pin in the areas where the corresponding rotors match up. What we could do though was to drill down further into the existing hole of the rotor and use a longer knock-pin. The stock knock pin is .795″ in length – exactly the same as the hole in the rotor. The stock hole and knock-pin bottomed-out at the transition of the aluminum and the steel magnets of the alternator. Getting the knock-pin hole deeper and using a longer pin allowed us to get down into the very hard steel of the alternator’s plate magnets. Drilling deeper required a vertical milling machine, the Bridgeport Mill gave us the .200″ that we wanted.
Forget using a drill bit and drill. This is a machine-shop repair. The metal used in those plate magnets is hardened and required a chucking reamer in size .3270 (MSC part # 02033272. The extra long knock-pins were made from drill stock/reamer blank in size 21/64 (.3281) in 5″ length (MSC part # 01100213). That size was large enough to remove all of the original hole’s wear and damaged area but would not exceed the clearance of the surrounding components. Again, this material is tool steel – the same as used in making drill bits.
We installed the longer knock-pins with Red Loctite (permanent type for steel) while the new 6mm countersunk machine screws were assembled and torqued to 90 in/lbs using Blue Loctite.